We thought that a trip down to Dorset, around 250 miles in total, would exercise the car nicely.
Luggage loaded easily, as the boot has reasonable space and there is quite a lot of room behind the seats for squashy bags.
The route down was via a section of the M3 and then through Salisbury. The car is very noisy at motorway speeds so single carriageway roads are much more relaxing, even though there were several hold-ups in which the car threatened to overheat. The car seemed to get noisier, particularly on the overrun and I made a note to investigate when we arrived back home.
We were both extremely tired when we arrived after about 2.5 hours and with hindsight may have been breathing a tad too much CO.
We stayed for 3 days at in lovely cottage about 2 miles inland from Durdle Door.
The weather was good, and we drove into Weymouth and to visit friends who have a cottage nearby.
I decided to drive back via the M27 and (slower, 60ish mph) along a short section of M3, stopping for lunch at Hinton Ampner, a NT property between Winchester and Petersfield. A lovely place, grand house and fantastic gardens.
Then things started to go badly wrong. The car started to misfire under light load, and the noise increased. Finally, about 20 miles from home, on the A31 near Alton, the Y connector between the exhaust manifold and straight pipe failed, dropping the front of the straight pipe section on the road. I was able to coast into a layby which was fortunately very close, looked at the options and called the RAC. Helpful chap turned up after about 45 minutes and tried to lift the pipe up using plastic cable ties.... I pointed out that these would melt so he added a bit of wire onto the gearbox mount. He then suggested that we drove to Farnham and try an exhaust centre. We drove a few miles, slowly, with the RAC van following. The car was incredibly noisy, lots of misfiring and backfiring and of course fumes all around. So I pulled into the car park of the Bull pub near Bentley and asked the RAC to send a tow truck.
So we sat in the pub garden and drank tea until the tow truck arrived about an hour later. The driver was a real star and took great care of the car which I drove onto the tilted flatbed. We were then driven back to Camberley.
So, this morning, Paul from Swiss Cottage (see the first blog post!) collected the car with his usual efficiency, and took the car to Lakeside. Max confirmed that that a weld on the (new) Y-section had failed, so a new one will be ordered and fitted, hopefully in the next couple of days.
With a bit of hindsight, it's obvious that the section had been starting to crack, hence the noise and fumes on the way down. The misfiring just before the exhaust failed was due to lower back pressure messing up mixture, timing, etc.